mirror of
https://github.com/torvalds/linux.git
synced 2026-05-24 15:12:13 +02:00
ARM: dts: imx6: RDU2: reduce i2c drive-strength
The current 25 Ohm drive-strength is much too strong, resulting in significant overshoot of the signal. Reduce the drive-strength to 75 Ohm to get rid of those issues. Signed-off-by: Lucas Stach <l.stach@pengutronix.de> Signed-off-by: Shawn Guo <shawnguo@kernel.org>
This commit is contained in:
parent
45a63cb559
commit
a0c01b68fd
|
|
@ -984,22 +984,22 @@ MX6QDL_PAD_EIM_D23__GPIO3_IO23 0x1b0b0
|
|||
|
||||
pinctrl_i2c1: i2c1grp {
|
||||
fsl,pins = <
|
||||
MX6QDL_PAD_CSI0_DAT8__I2C1_SDA 0x4001b8b1
|
||||
MX6QDL_PAD_CSI0_DAT9__I2C1_SCL 0x4001b8b1
|
||||
MX6QDL_PAD_CSI0_DAT8__I2C1_SDA 0x4001b811
|
||||
MX6QDL_PAD_CSI0_DAT9__I2C1_SCL 0x4001b811
|
||||
>;
|
||||
};
|
||||
|
||||
pinctrl_i2c2: i2c2grp {
|
||||
fsl,pins = <
|
||||
MX6QDL_PAD_KEY_COL3__I2C2_SCL 0x4001b8b1
|
||||
MX6QDL_PAD_KEY_ROW3__I2C2_SDA 0x4001b8b1
|
||||
MX6QDL_PAD_KEY_COL3__I2C2_SCL 0x4001b811
|
||||
MX6QDL_PAD_KEY_ROW3__I2C2_SDA 0x4001b811
|
||||
>;
|
||||
};
|
||||
|
||||
pinctrl_i2c3: i2c3grp {
|
||||
fsl,pins = <
|
||||
MX6QDL_PAD_GPIO_3__I2C3_SCL 0x4001b8b1
|
||||
MX6QDL_PAD_GPIO_6__I2C3_SDA 0x4001b8b1
|
||||
MX6QDL_PAD_GPIO_3__I2C3_SCL 0x4001b811
|
||||
MX6QDL_PAD_GPIO_6__I2C3_SDA 0x4001b811
|
||||
>;
|
||||
};
|
||||
|
||||
|
|
|
|||
Loading…
Reference in New Issue
Block a user